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  • Well Control Help

    Well was displaced with 15.2ppg brine prior to set 7” tie back packer was set @ 4510 & new TOL 4497m.

    RIH TCP guns & perforate overbalanced with 15.2ppg brine (expected pressure was 14.9ppg formation pressure) f/5217.5-5233.5 & 5256.5-5265m.

    Observe 200psi on choke manifold, shut well & observe pressure increase to 560psi. SICP-295 & SIDP 221psi. Before shutting well SICP-335 & SIDP-647.

    Circulate #1 well with drillers method OBSERVED INITIAL SICP 304 PSI & SIDPP 574 PSI, observe 14.08% of gas at surface. Stop circulation & monitor well. SICP 326psi & SIDP 300psi. Bleed of ¾ bbl through choke & obs SICP-250 & SIDP 237psi. Shut well & monitor well, SICP–400psi & SIDP–376psi.

    Begin #2 circulation with 15.2ppg brine through down the string & up the choke. SIDPP- 700psi and SICP-367psi. Max gas observed 11.85%. Last recorded pressures Drill pipe 685psi casing pressure 317 psi. Shut in well on choke and observed for pressure buil up. SIDPP-532psi, SICP-518psi. FIRST Bleed off 0.75bbls , DP -211PSI, CP-205PSI. Shut in well on choke and observed for pressure buil up. SIDPP-347psi, SICP-348psi. SECOND Bleed off 0.75bbls
    sicp-105psi, sidpp-107psi.

    Shut well, Pressure increased to sicp-180psi, sidpp-180psi. Bleed off 3/4bl. sicp-41psi, sidpp-41psi. 2100-2200 shut in well to observe pressure build up. sicp-64psi, sidpp-55psi. bled off 1 1/4bbl. sicp-12psi, sidpp-25psi. Shut in well to observe pressure build up. sicp-27psi. sidpp-27psi.

    #3rd circulation of driller’s method. initial pressure: sicp-150psi, sidpp-476psi. max gas observed 22.2% after bottoms up. further circulation is in progress.


    To balance current well control situation required brine weight is 15.5ppg & overbalance is 15.6ppg. Chemicals to prepare higher ppg brines are not available & also well cannot be displaced with available SOBM mud as the 7” tie back packer is not compatible with SOBM mud.


    Do any one have any solution for this situation
    This article was originally published in forum thread: Well Control Help started by himansh1990 View original post
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